Enron Mail

From:drew.fossum@enron.com
To:keith.petersen@enron.com
Subject:Gallup - Status Update, May 4, AM
Cc:mary.miller@enron.com
Bcc:mary.miller@enron.com
Date:Wed, 3 May 2000 03:39:00 -0700 (PDT)

Please call when you've reviewed this. Thanks. DF
---------------------- Forwarded by Drew Fossum/ET&S/Enron on 05/03/2000=20
10:36 AM ---------------------------
=20
=09
=09
=09From: Susan Scott 05/03/2000 08:46 AM
=09

To: Drew Fossum@ENRON, Donna Martens/ET&S/Enron@ENRON
cc: =20

Subject: Gallup - Status Update, May 4, AM

FYI
---------------------- Forwarded by Susan Scott/ET&S/Enron on 05/03/2000=20
08:44 AM ---------------------------


James Pfeffer@ENRON_DEVELOPMENT
05/03/2000 08:00 AM
To: Michel Nelson/ET&S/Enron@ENRON, John R Keller/OTS/Enron@Enron, Ray=20
Smith/ET&S/Enron@ENRON, Lorraine Lindberg/ET&S/Enron@ENRON, Arnold L=20
Eisenstein/ENRON_DEVELOPMENT@ENRON_DEVELOPMENT, Steven=20
Harris/ET&S/Enron@ENRON, James Pfeffer/ENRON_DEVELOPMENT@ENRON_DEVELOPMENT,=
=20
Rich Jolly/ET&S/Enron@ENRON, Jeffery Fawcett/ET&S/Enron@ENRON, Rich=20
Plachy/Enron Communications@Enron Communications, David=20
Roensch/ET&S/Enron@ENRON, Team Gallup/ET&S/Enron@ENRON, Ronald=20
Matthews/ET&S/Enron@ENRON, Earl Chanley/ET&S/Enron@Enron, Vera=20
Jones/ET&S/Enron@ENRON, Brian H Mellon/ENRON_DEVELOPMENT@ENRON_DEVELOPMENT,=
=20
John G Keller@EES, Phil Lowry@ENRON, Darrell Schoolcraft@ENRON, Susan=20
Scott@ENRON, Kevin Hyatt@ENRON
cc: =20

Subject: Gallup - Status Update, May 4, AM

The suction strainer was removed last night. The piping spool was=20
reinstalled without the major compressor alignment problems that were=20
expected. This significantly reduced the downtime necessary for the remova=
l=20
of the suction strainer.

No major foreign materials were found in the strainer. Some small weld bea=
ds=20
were found. There were some signs that the strainer may have been vibratin=
g.

Several compressor test runs were made early this AM to measure the vibrati=
on=20
levels without the suction strainer. The high frequency vibration was=20
reduced to safe levels. There is no longer any risk to the unit piping=20
integrity.

The compressor bearing vibration did not decrease due to the removal of the=
=20
strainer. Rolls will continue to assess the collected vibration data to=20
determine the cause of the high drive end bearing vibration and construct a=
=20
game plan.

The station once again became available for service around 4 AM. The=20
compressor may or may not be run dependent on need. Gallup Ops and Gas=20
Control are in close contact.

The station will be manned if the compressor is running due to Gas Control=
=20
being unable to send remote setpoints to the station controller. The probl=
em=20
stems from OPTO-22 not supporting the particular Modbus function required t=
o=20
send setpoints. This is a =01+lack of functionality=01, in the new LCM4 ve=
rsion=20
controllers/software utilized on the Gallup Project. =20

EECC has been in contact with OPTO-22 to determine the time table for=20
resolving this problem. EECC, TW Ops are working on a temporary fix to=20
enable Gas Control to send remote setpoints to Gallup. Gas Control is=20
currently able to monitor data from Gallup.

Some instrumentation will be replaced today that failed due to the high=20
vibration over the fast few days.

Final tuning of the station control loops and surge control will be also be=
=20
conducted today.

James Pfeffer